When I left off in May of 2022(is that possible?), the truck was running good and I had a few things to button up. For one, the front passenger axle seal was still leaking. I had replaced it twice and I tried one more time before I had to admit defeat and take it to a shop. I took it to the dealership because I also had 2 blank key fobs I wanted to get programmed. I no longer have a leak, nor do I have to manually unlock my doors like a peasant.

The oil pan was leaking again, so I went through and one at a time took every bolt out, cleaned it and retorqued it with Blue Loctite. It has been leak free for the past 22 months.

Where I had thought that the rear differential was leaking, it was just oil blowing from the oil pan. I changed the fluid anyway and put a new gasket in. The gears all looked pristine. I was planning on changing the fluid and gasket with my last big project, but had forgot with everything else I did. Also, the transmission was getting a little difficult to put into 1st or reverse while stopped, so I changed the gear oil and put in new gaskets, so she shifts much easier.

It seemed a little laggy when I was trying to accelerate, so I did a boost leak test. To do this, I clamped a special boot on the inlet of the turbo and hooked up my air compressor which I set to 10psi. As soon as I did this, I heard air hissing out of the large snap ring that holds the main cover on.Stupid snap ring!On reassembly, apparently I didn’t fully seat it into its groove. Tapped a few times and it made a loud click and then the leak stopped. Took her for a drive and it felt better.

Drove her all over for the next few months and then it became obvious that the 100hp injectors with the Edge programmer were too much for the stock turbo. It was making a clicking noise and when I pulled the air cleaner it had excessive movement in the shaft and I could see where the compressor wheel was scraping on the side.

YIKES!

Well, guess I need a new turbo. With a manual transmission, I was worried about getting one that would take too long to spool. looking at options, I narrowed it down to Diesel Auto Power (DAP), Savage Fabrication, and Power Driven Diesel (PDD). They all offered similar drop in turbos that they all said would work really well for my application. All 3 were right around $1,300, but then PDD was having a sale and theirs was $1,000 so that’s the one I went with.

New one sure is purty

The stock HX 35 is 57/78mm compressor and 60mm turbine exducer, compared to PDD’s 60/80mm compressor and 64mm turbine exducer. It is designed to fit where a stock one does, so I didn’t have to change my exhaust manifold. Since I had pulled the stock turbo before to rebuild it, doing it again was easy. I did have to swap the rear piece that bolts to my exhaust and loosen all of the bolts that hold the turbo together so that I could align the oil fill, oil drain, and the air discharge pipe. Oiled it and spun the compressor wheel to ensure a good coat on the journal bearings.

SEXY!

I drove it some but took it easy for a few months to give the turbo a chance to break in. Then I took it on vacation up to my mom’s house by Pittsburgh. We put about 1200 miles on it and while I was happy with the performance, I wasn’t blown away like I expected to be. Still a lot of fun to drive though.

While we were there, I started to get a coolant leak from the A/C drain. Did some research and apparently this is a heater core leak. It was October 2022 and it wasn’t too cold, so I ran the 2 heater lines together and had no more leak. This didn’t cause any issues until the day we headed home and it was 30 degrees and cloudy. The truck was COLD. My wife was miserable and I was sitting on one hand until it warmed up and then swapping with the one on the steering wheel. Good times. When we stopped for lunch, it took awhile to warm up. Once we dropped out of the Allegheny Mountains, it was much more bearable.

Disassembly

In order to replace the heater core, you have to remove the entire dash. I bought a replacement dash from LMC along with an instrument bezel, because mine had a cover, so I figured underneath that, it was cracked. I then had my first genius idea that “As long as I’m in there” I might as well replace the 22 year old carpet, it was really ragged and stained.

What was I thinking?!?

 

It was easy enough to remove the seats and seat belt bolts.

Let the madness begin!

Now it was time to remove the dash and I was not surprised when I peeled the plastic cover off of my dash that underneath it was shattered.

Worse than I thought it would be

This was a job I had never done before, but following these instructions and this YouTube video it wasn’t as hard as I thought it would be. (Sidenote: The truck in the video is gorgeous, I love that color.) I became concerned about the lower dash when I put my electric screwdriver on the HVAC control screws and the plastic behind it exploded. I had heard of some people that pulled the dash and found the lower part to be unusable. I hoped that wasn’t going to be me.

Not as much fun as it looks

Changing the heater core was simple enough, I bought one with swivel lines from Geno’s Garage, all I had to do was put some foam tape around the outside and struggle with the lines to get the angle right until it somehow slid in. I have since heard of people having leaks from where the swivel joints are and wish I had known about a solid brass one that’s available. Even though it costs way more, if the one I put in leaks, I will buy the brass one, this is not a job to do anymore than absolutely necessary.

The thing that started this whole mess.

Now it was time to remove the upper dash from the plastic lower dash.

Why is it falling apart?

This was easy, because half of the upper dash was already gone. Problem was the lower dash kept breaking, no matter how careful I was with disassembly. Once I got the two halves separated, I bought a plastic welder so I could repair the lower dash. I tried to save it, but every time I fixed one section, another place would crack. I did not lose my cool, all I could do was laugh as the new cracks kept appearing. Out of all of the projects I have done on this truck, this is the first one that made me actively hate Dodge.

I finally had to give up and buy a used one off of Ebay for $1,000. It irritates me to type that. Once it showed up, it was solid and I was able to screw it to the metal frame with no problem.

It was at this point I had my second genius idea: “As long as I’m in there” I never did like the gray, why don’t I paint it black? So I removed all of the interior plastic.

Seriously, Why didn't someone stop me?

As soon as I had all of the plastic pieces pulled out, I felt like G.O.B. from Arrested Development, I’ve made a huge mistake“. The gray wasn’t that bad, was it? Oh well, nothing to do now but keep going. I bought some black plastic paint and adhesion promoter from LMC that had been recommended by people on the Cummins Forum. First, I washed all the plastic pieces with dish soap and once they dried, I wiped them down with rubbing alcohol.

Immediately before painting each piece, I wiped them down with rubbing alcohol again and gave them a good layer of the adhesion promoter. Once that dried a little I gave them 3 or 4 coats of the black paint. This stuff laid down amazingly well. It looked as though they were black and not gray painted black which I had feared.

Looks as good as I hoped

 

This felt like it took forever

 

Lot of work for this

Now it was time to paint the dash itself. I had received it three months prior and had only opened the box enough to verify the color and get an idea what the quality was like. When I pulled the whole thing out, my heart sank. The little point of the dash was snapped off.

You have got to be kidding me!

I called LMC, fully expecting to have to buy another dash. I told them what happened and explained that the box was undamaged, so I might have broken it, but I doubted it. I also told them that it had been sitting in its original box for three months and I hadn’t pulled it out until today. They had me send them a picture and once they reviewed it, they sent me a free replacement. Honestly, if they had agreed to sell me one half off I would have been ecstatic.

While I was waiting for the new dash, I pulled out the old raggedy carpet. I had ordered a vinyl carpet from OC Auto Carpets a few months ago and still had it in the box.

It was a lot of work to get to this point and now I had the task of putting everything together waiting for me. That will be covered in the next installment.

For music, I will post one of my favorites to listen to while I’m in the garage, Shooter Jennings.

4th of July

D.R.U.N.K.

Rhinestone Eyes